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94 Commits

Author SHA1 Message Date
Jason ddcc03d89c chirp-v2 PR-F follow-up 2: TB widenings + 50T include + comment
Closes the four deferred items from project_chirp_v2_pr_f_review_followups
that were carved out of 51a94f0 to keep that diff narrow.

A. TB doppler_bin / dbg_doppler_bin / dbg_range_bin still 5 / 6 bits,
   ports widened to 6 / 9 in PR-F:
     - tb/tb_doppler_cosim.v
     - tb/tb_doppler_frame_start_gate.v
     - tb/tb_system_e2e.v
     - tb/radar_system_tb.v
     - tb/tb_radar_receiver_final.v
   All five files now include radar_params.vh and use
   `RP_DOPPLER_BIN_WIDTH / `RP_RANGE_BIN_WIDTH_MAX. tb_doppler_cosim.v
   was already structured around CHIRPS=32 and would have stalled
   forever against the new 48-chirp default — added explicit parameter
   overrides (CHIRPS_PER_FRAME=32, CHIRPS_PER_SUBFRAME=16, RANGE_BINS=512)
   to keep its legacy 2-subframe golden vectors valid, mirroring the
   pattern already used by tb_doppler_realdata / tb_fullchain_realdata.

B. tb_radar_receiver_final hardcoded NUM_DOPPLER_BINS=32 across the
   golden buffer, the per-range bitmap, the duplicate-detect mask, the
   gidx multiplier, and the S5/S6/S7/B3/B4 expected counts. All bumped
   to `RP_NUM_DOPPLER_BINS (=48) via NUM_DBINS / NUM_RBINS / GOLDEN_ENTRIES
   localparams; per-range index_seen widened to 64-bit so
   `(64'd1 << doppler_bin)` covers bins 32..47. Note: under iverilog the
   doppler-frame checks (S4-S9, B2a, B3, B4, G1) remain gated on
   FFT_USE_XILINX_IP — the in-house fft_engine is too slow to land a
   48-chirp Doppler frame in 20 ms sim; under XSim with the IP the
   widened logic now exercises the full 24576-cell output (was 16384).
   The 8-test active subset under iverilog is unchanged.

C. radar_system_top_50t.v adds `\`include "radar_params.vh"`, which is
   needed for the `\`RP_DOPPLER_BIN_WIDTH-1:0]` reference added in PR-F.
   Previously worked only because alphabetical Vivado file ordering
   processes radar_system_top.v (which does include) first and the
   macros leak across the same compilation unit. While here, also bumps
   the dbg_range_bin_nc tie-off wire from a literal [5:0] to
   `RP_RANGE_BIN_WIDTH_MAX-1:0] so the wrapper width matches the port.

D. usb_data_interface_ft2232h.v:392 stale comment ("FRAME_CELLS = 24576
   < 32768") rewritten to reflect that PR-F's pad-to-power-of-2 makes
   FRAME_CELLS = NUM_RANGE_BINS * (1<<DOPPLER_BIN_BITS) = 32768 (the
   full 15-bit address space).

Tests (parity with PR-F baseline numbers in 7862f4d / 51a94f0):
  - tb_doppler_cosim (3 scenarios): 14/14 each + Python golden compare PASS
  - tb_doppler_frame_start_gate:    21/21 PASS
  - tb_doppler_realdata:            2056/2056 PASS
  - tb_cfar_ca:                     24/0  PASS
  - tb_chirp_controller:            43/43 PASS
  - tb_chirp_contract:              10/10 PASS
  - tb_mti_canceller:               43/43 PASS
  - tb_radar_receiver_final:        8/8   PASS
  - tb_system_e2e:                  33/49 PASS
  - radar_system_tb (USB_MODE=1):   smoke (no PASS/FAIL markers; runs to $finish)
  Lint (iverilog -Wall on full PROD_RTL + 50t wrapper): no new
  width / Padding / Truncating warnings introduced.
2026-05-01 04:35:08 +05:45
Jason 7862f4d63c chirp-v2 PR-F: doppler/CFAR widen to 3 sub-frames + 2-class detect
Bumps RP_CHIRPS_PER_FRAME 32 -> 48 (= 3 sub-frames × 16 chirps), widens
doppler_bin from 5 to 6 bits ({sub_frame[1:0], bin[3:0]}), and replaces the
1-bit detect_flag rail with a 2-bit detect_class (NONE / CANDIDATE /
CONFIRMED) sourced from a soft+confirm CFAR threshold pair.

doppler_processor:
  Generalised the 2-subframe FSM to NUM_SUBFRAMES = CHIRPS_PER_FRAME /
  CHIRPS_PER_SUBFRAME (=3 in production, =2 when TBs override). S_OUTPUT
  walks current_sub_frame 0..NUM_SUBFRAMES-1 then advances range_bin;
  the chirp_base * CHIRPS_PER_SUBFRAME formula replaces the if/else split.
  write_chirp_index, read_doppler_index, sub_frame, current_sub_frame all
  widened to 6/2 bits accordingly. doppler_bin packing {current_sub_frame[1:0],
  fft_sample_counter[3:0]} naturally yields 6 bits.

cfar_ca:
  Adds cfg_alpha_soft input + r_alpha_soft register (default
  RP_DEF_CFAR_ALPHA_SOFT = 0x18 ≈ 1.5 in Q4.4 → Pfa_soft ≈ 1e-5). ST_CFAR_MUL
  computes both noise_product (alpha) and noise_product_soft (alpha_soft) in
  parallel DSPs; ST_CFAR_CMP emits detect_class = CONFIRMED when cur > thr,
  CANDIDATE when cur > thr_soft (and not CONFIRMED), NONE otherwise.
  detect_flag is preserved as (class != NONE) for backward compat.
  Address packing now pads doppler axis to next power-of-2 (DOPPLER_PAD =
  1 << ceil(log2(NUM_DOPPLER))) so {range, doppler} packs contiguously
  for both NUM_DOPPLER=32 (legacy TB) and NUM_DOPPLER=48 (production).
  Mag-BRAM grows from ~16 to ~30 RAMB18 on 50T (acceptable on the budget).

usb_data_interface_ft2232h:
  doppler_bin_in widened to 6 bits. FRAME_CELLS pads to next power of two
  (32K) so {range, doppler[5:0]} concatenation lands cleanly. Address regs
  bumped: mag_wr/rd_addr 14→15, detect_byte_addr 11→12, detect_clear bit-
  counter 14→15. Detect-bit BRAM grows 2K→4K bytes. Wire-protocol byte
  counts auto-scale with FRAME_CELLS / DOPPLER_MAG_SECTION_BYTES; PR-G
  bumps the bulk-frame protocol version so the host parser knows.

Other:
  - radar_params.vh: RP_CHIRPS_PER_FRAME 32→48, RP_NUM_DOPPLER_BINS 32→48,
    RP_DOPPLER_MEM_ADDR_W 14→15 (50T) / 17→18 (200T), RP_CFAR_MAG_ADDR_W
    likewise. Other macros (RP_DOPPLER_BIN_WIDTH=6, RP_DETECT_CLASS_WIDTH=2,
    RP_DEF_CFAR_ALPHA_SOFT=0x18, RP_NUM_SUBFRAMES=3) were already in place
    from PR-A.
  - radar_system_top: rx_doppler_bin / dbg_doppler_bin widened. Adds
    host_cfar_alpha_soft register (default RP_DEF_CFAR_ALPHA_SOFT). USB
    opcode mapping deferred to PR-G.
  - radar_system_top_50t: dbg_doppler_bin_nc width.
  - radar_receiver_final: doppler_bin port width.

Test summary:
  - tb_chirp_controller_v2:  43/43 PASS
  - tb_chirp_contract:       10/10 PASS
  - tb_cfar_ca:              24/0 PASS
  - tb_mti_canceller:        43/43 PASS
  - tb_rxb_fullchain:        peak 24033 ~80x (parity with PR-D/E)
  - tb_doppler_realdata:     2056/2056 PASS  (had been broken pre-PR-F due
                             to missing RANGE_BINS=64 override; this PR fixes
                             the parameter override along with the widening)
  - tb_system_e2e:           33/49 PASS — identical to PR-E baseline; the
                             one new fail vs PR-D (G2.2) carries over.
  - tb_radar_receiver_final: still finishing in background (~10 min).
2026-05-01 03:36:03 +05:45
Jason a1a8fa7107 chirp-v2 PR-E: plfm_chirp_controller_v2 + scheduler-driven TX via async-FIFO
Replaces plfm_chirp_controller_enhanced (5-state FSM with hardcoded
LONG/SHORT timings + 60-entry inline short LUT) with plfm_chirp_controller_v2,
a pure DAC playback driver: IDLE -> CHIRP -> IDLE keyed off a 1-cycle
dst_chirp_valid pulse, with sample count selected by dst_wave_sel
(SHORT=120 / MEDIUM=600 / LONG=3600). Inter-chirp timing (LISTEN, GUARD,
frame boundaries) is now owned exclusively by chirp_scheduler.

Scheduler -> TX bridge: cdc_async_fifo (Cummings style #2, WIDTH=2 DEPTH=4)
crosses {wave_sel} from clk_100m to clk_120m_dac, with chirp_pulse as
src_valid. frame_pulse rides a separate toggle CDC for chirp_counter
clear and the new_chirp_frame status output. mixers_enable now also gates
the scheduler so it stays in S_IDLE while the radar is "off" — without
this gate the first chirp_pulse fires at reset and gets dropped before
mixers come up.

Files:
- NEW  plfm_chirp_controller_v2.v      DAC playback driver (3 LUTs, FSM)
- DEL  plfm_chirp_controller.v         legacy controller (382 lines)
- DEL  long_chirp_lut.mem              legacy LUT (3600 lines), replaced
                                       by tx_long_lut.mem from PR-B
- chirp_scheduler.v       + mixers_enable input (master quiesce)
- radar_receiver_final.v  + sched_*_out output ports + mixers_enable_100m
- radar_system_top.v      wire sched_*_out -> tx_inst.sched_*; pass
                          stm32_mixers_enable_100m to rx_inst
- radar_transmitter.v     full rewrite: drop new_chirp edge detector +
                          toggle CDC, instantiate cdc_async_fifo for
                          {wave_sel}, toggle CDC for frame_pulse,
                          plfm_chirp_controller_v2 in place of _enhanced
- tb/tb_chirp_controller.v  + tb/tb_chirp_contract.v  rewritten for v2
                          contract (43/43 unit + 10/10 contract green)
- tb/tb_radar_receiver_final.v  + .mixers_enable_100m(1'b1) pin
- run_regression.sh, scripts/200t/build_200t.tcl  file-list bumped

Test summary:
- tb_chirp_controller_v2:   43/43 PASS
- tb_chirp_contract:        10/10 contracts upheld
- tb_rxb_fullchain:         peak 24033 ~80x (parity with PR-D)
- tb_mti_canceller:         43/43 PASS
- tb_system_e2e:            33/49 (1 new vs 34/49 PR-D baseline: G2.2
                            new_chirp_frame, intentional v2 frame-pulse
                            semantics — fires once per Doppler frame
                            instead of once per stm32 chirp toggle.
                            TB needs widening in PR-H to wait the full
                            frame.)
2026-04-30 21:51:46 +05:45
Jason 8e8f3e60c4 chirp-v2 PR-D: chirp_scheduler replaces radar_mode_controller; MF/MTI wave_sel-native
Single 100 MHz scheduler emits wave_sel[1:0] and chirp_pulse natively. Modes
00 (STM32 pass-through), 01 (auto-scan over SHORT/MEDIUM/LONG sub-frames),
10 (single-chirp debug), 11 (track dwell with watchdog scan-fallback after
RP_DEF_TRACK_WATCHDOG_FRAMES=5 idle frames). Sub-frame mask lets ops drop a
waveform without recompiling.

Drops the receiver_final wave_sel shim added in PR-C: wave_sel comes
straight from the scheduler; chirp_pulse replaces the old mc_new_chirp
toggle + XOR edge converter. matched_filter_multi_segment and mti_canceller
take wave_sel[1:0] and chirp_pulse directly — no parallel paths.

multi_segment also bumped: SHORT_CHIRP_SAMPLES 50 -> 100 (V2 1 us SHORT)
and MEDIUM_CHIRP_SAMPLES = 500 (5 us). LONG path unchanged. Dead
mc_new_elevation/azimuth XOR converters removed.

Deletes radar_mode_controller.v, formal/fv_radar_mode_controller.v, and
tb/tb_radar_mode_controller.v. Build manifests (run_regression.sh,
scripts/200t/build_200t.tcl) updated. Receiver_final pins medium/track/
subframe_enable inputs to RP_DEF_* defaults until PR-G plumbs USB opcodes.

Verification:
- tb_rxb_fullchain_latency: peak |I|+|Q|=24033 at bin 0, ~80x peak/mean
  (up from PR-C's 15115 since matched filter now uses full 100 SHORT samples)
- tb_mti_canceller: 43/43 PASS with new wave_sel[1:0] input
- tb_radar_receiver_final: 8/8 PASS, ALL TESTS PASSED
- tb_system_e2e: 34/49 PASS - identical to pre-PR-D baseline (15 failures
  are pre-existing matched-filter cycle-budget skips); G8.2/G8.3 chirp_scheduler
  probes PASS
- tb_multiseg_cosim: 16/32 - same as pre-PR-D baseline
2026-04-30 20:52:32 +05:45
Jason 4238eb1b99 chirp-v2 PR-C: chirp_reference_rom replaces chirp_memory_loader_param
Drop the chirp-v1 1-bit use_long_chirp memory loader and its 6 .mem files;
introduce chirp_reference_rom — wave_sel-native, single 8192x16 BRAM array
per Q15 lane, 4-region init (SHORT, MEDIUM, LONG seg0/seg1) loaded from the
PR-B mem files. Same 1-clk read latency as the legacy module so the RX-B
autocorrelation alignment fix carries through unchanged.

Receiver-side wave_sel shim added in radar_receiver_final.v:
  wire [1:0] wave_sel = use_long_chirp ? RP_WAVE_LONG : RP_WAVE_SHORT;
This is a 1-line transitional bridge while radar_mode_controller still
emits 1-bit use_long_chirp; PR-D deletes the shim and wires chirp_scheduler
straight through. MEDIUM is loaded into the ROM but unreachable through
the production path until PR-D.

BRAM cost: 8 RAMB18 (was 6 in chirp-v1). +2 BRAM is the cost of adding
MEDIUM to the waveform set; not avoidable.

Files added:
  - chirp_reference_rom.v
Files removed:
  - chirp_memory_loader_param.v
  - long_chirp_seg{0,1}_{i,q}.mem (4 files)
  - short_chirp_{i,q}.mem (2 files)
  - tb/cosim/validate_mem_files.py (legacy file-set validator; replaced by
    gen_chirp_mem.py's internal verify_phase_match)
  - tb/cosim/analyze_short_chirp_mismatch.py (one-shot tool from the
    chirp-v1 TX-I investigation; finding incorporated, references the
    deleted short_chirp_*.mem files)
Files updated for module rename:
  - radar_receiver_final.v        — instance, comments, wave_sel shim
  - radar_mode_controller.v       — header comment
  - matched_filter_processing_chain.v — header comment
  - scripts/200t/build_200t.tcl   — explicit RTL list
  - run_regression.sh             — 5 spots
  - tb/tb_rxb_fullchain_latency.v — instance, wave_sel shim, mem filenames,
                                    SHORT_LEN 50 → 100 (1 µs at 100 MHz)
  - tb/tb_system_e2e.v            — header comment

Verification:
  - chirp_reference_rom standalone iverilog compile: clean
  - Full receiver chain compile (21 RTL files): clean
  - tb_rxb_fullchain_latency runs end-to-end with new ROM + new mem files
    + 100-sample SHORT chirp; autocorrelation peak at bin 0, peak |I|+|Q|
    = 15115. Confirms 1-clk ROM read latency is preserved and the RX-B
    direct-wire-with-1-FF alignment still holds.
  - 50T build script (scripts/50t/build_50t.tcl) uses glob *.v — no edit
    needed; it picks up the new file automatically.
2026-04-30 19:37:43 +05:45
Jason f5b8e7a20b chirp-v2 PR-B: 3-waveform mem generator + 11 new .mem files
Rewrite gen_chirp_mem.py to emit the SHORT (1 µs), MEDIUM (5 µs), and LONG
(30 µs) waveform set on both TX and RX paths. The script is now the single
source for every chirp .mem file; the legacy 6-file set on disk
(long_chirp_lut.mem, long_chirp_seg{0,1}_{i,q}.mem, short_chirp_{i,q}.mem)
is no longer regenerated and gets deleted in PR-C/PR-E when its consumer
modules are removed.

Generated artifacts (committed):
  TX (8-bit unsigned offset-binary, fs_dac = 120 MHz):
    tx_short_lut.mem    120  lines
    tx_medium_lut.mem   600  lines
    tx_long_lut.mem     3600 lines
  RX (Q15 I/Q hex, fs_sys = 100 MHz, all 2048 lines for uniform BRAM sizing):
    rx_short_i.mem  / rx_short_q.mem    100  active + 1948 zero-pad
    rx_medium_i.mem / rx_medium_q.mem   500  active + 1548 zero-pad
    rx_long_seg0_i.mem  / rx_long_seg0_q.mem   2048 (samples [0..2047])
    rx_long_seg1_i.mem  / rx_long_seg1_q.mem   952 active + 1096 zero-pad

Phase model unchanged from chirp-v1: phi(n) = 2π·F_BASEBAND_LOW·t +
π·(BW/T)·t² with F_BASEBAND_LOW=10 MHz and BW=20 MHz. The same formula now
runs three durations and two sample rates from one helper.
rx_long_seg0_i.mem is bit-exact to the legacy long_chirp_seg0_i.mem on disk
(diff -q reports identical) — proves the SHORT/MEDIUM additions did not
perturb the LONG path.

Verification:
  - all 11 files have correct line counts (above)
  - script is idempotent (re-run produces byte-identical output)
  - ruff clean (one E501 line-length + two RUF046 redundant-int casts fixed)
  - phase regression at long-seg0 against pre-chirp-v2 reference: bit-exact

No RTL or testbench changes. The legacy .mem files remain on disk for the
existing chirp_memory_loader_param.v / plfm_chirp_controller.v consumers
until PR-C and PR-E delete those modules. No module references the new
files yet.
2026-04-30 17:46:08 +05:45
Jason 58d2e1ba10 AUDIT-C11: replace Gray-CDC at CIC→FIR with home-grown async FIFO
cdc_adc_to_processing carries multi-bit data across 400→100 MHz via
TWO independent synchronizer chains (data Gray-encoded + a separate
2-bit toggle). Under metastability, the chains can resolve on
different cycles, letting the destination latch a half-resolved Gray
word that decodes to an arbitrary value. Audit C-11. Practical MTBF
is years per event but the design is non-conformant for arbitrary
multi-bit data — Gray code's single-bit-flip protection only holds
for ±1 transitions, not for CIC samples that can change by hundreds
of LSBs.

Replace with cdc_async_fifo, a Cummings SNUG-2002 style #2 async
FIFO. Data does NOT cross domains; it sits in dual-clock distRAM
(write port src_clk, read port dst_clk). Only the read/write
Gray-coded POINTERS cross — and pointers genuinely change ±1 per
increment, so Gray code's protection is correct by construction.
Home-grown rather than XPM_FIFO_ASYNC: vendor-neutral (iverilog can
simulate it directly, no SIM stub), keeps the project's existing
home-grown CDC convention (3 sibling primitives in cdc_modules.v),
and avoids XPM library version skew.

Port shape is preserved (same WIDTH=18, same dst_data/dst_valid/
overrun semantics — 1-cycle pulse per read in steady state) so the
swap is local to two instantiations in ddc_400m.v. Sticky-overrun
aggregation downstream is unchanged.

XDC: project already has blanket set_false_path on
clk_100m ↔ adc_dco_p, which covers both new pointer crossings.
Synchronizer FFs carry ASYNC_REG="TRUE" for placement-aware MTBF.
No XDC change needed.

New TB tb_cdc_async_fifo.v exercises 7 groups (28 checks): reset,
single-sample passthrough, multi-Gray-bit-flip (0x00000 ↔ 0x3FFFF —
audit's recommended coverage point, asserts NO intermediate values
appear at dst_data), matched-rate continuous stream, sustained-burst
overrun, drain-to-empty, and mid-stream reset.

Resource: 8 LUTRAMs per instance × 2 instances = 16 LUTRAMs (~0.05%
of XC7A50T budget).

Verified: full FPGA regression 42/42 PASS (was 41/41; +1 new test,
0 regressions in DDC Chain / Doppler Co-Sim / Full-Chain Real-Data
/ Receiver Integration / System Top / System E2E / MF Co-Sim — all
of which exercise the swap path through the production signal
chain). 0 lint errors.
2026-04-30 10:47:31 +05:45
Jason 853d2a5fd9 AUDIT-S19/S20/S21: replace fpga_self_test tautologies with real arithmetic
Pre-fix Tests 1/2/4 in fpga_self_test.v gave false PASS even on broken
silicon:

  S-19 Test 1 (CIC): `result_flags[1] <= 1'b1` unconditional, comment
       admitted "always true for simple check".
  S-20 Test 2 (FFT): `(16'sd100+16'sd100 == 16'sd200) && (...)` —
       both predicates compile-time-fold to 1; synth reduces to a
       constant write.
  S-21 Test 4 (ADC): PASS once N samples land, regardless of value.
       A stuck-at-0 / stuck-at-MAX / dead LVDS link still PASSed
       provided adc_valid_in toggled.

Fixes:

  Test 1: drive impulse {5,0,0,0,0,0,0} through registered integrator
          y[n]=y[n-1]+x[n]; require accumulator==5 after step
          response. Real adder + register path; sign-extension
          exercised. Detail = 0xC1 on fail.

  Test 2: real radix-2 butterfly with twiddle multiply across 4 FSM
          states. A=8, B=4 (real), W=2+3j -> WB=(8,12), A'=(16,12),
          B'=(0,-12). Forces synth to instantiate signed multiplier
          (DSP slice) + 17-bit signed add/sub. Detail = 0xF2 on fail.

  Test 4: track min/max across 256-sample capture, require
          (max - min) > ADC_RANGE_THRESHOLD (10 LSB). Catches stuck-at
          faults. Does NOT distinguish AD9484 format mismatches
          (audit's per-mode mean check requires SPI, impossible per
          AUDIT-C13). Detail = 0xAD on fail.

Tests:
- tb_fpga_self_test.v existing Group 1-4 (16 PASS) still pass: varied
  ADC counter input gives range >> 10.
- New Group 5: drive constant 0 -> expect Test 4 FAIL + detail=0xAD.
- New Group 6: drive constant 0x7FFF -> expect Test 4 FAIL + detail=0xAD.
- Regression: 41/41 PASS; fpga_self_test 22/22 (was 16/16).
2026-04-29 23:27:15 +05:45
Jason 9bed35287a AUDIT-C16: parameterize NUM_CELLS + sample_counter width for 200T
Pre-fix usb_data_interface.v hardcoded `localparam [14:0] NUM_CELLS =
15'd16384` for the 50T 512-range x 32-doppler layout. On 200T builds
with SUPPORT_LONG_RANGE defined, RP_MAX_OUTPUT_BINS=4096 makes a real
frame 131072 cells, so the fixed value caused two distinct defects:

  (a) value: counter wrapped 8x per real frame; bit-7 frame-start
      marker fired 8x at incorrect host-frame offsets, silently
      desyncing the GUI parser
  (b) width: 15 bits could not represent 131072 (needs 17 bits)

Fix: derive NUM_CELLS = RP_MAX_OUTPUT_BINS * RP_NUM_DOPPLER_BINS and
counter width = RP_DOPPLER_MEM_ADDR_W (14 on 50T, 17 on 200T) from
radar_params.vh, so both scale together with the build define.

Tests:
- tb_audit_c16_num_cells.v: standalone counter-block exerciser (T1
  reset, T2 increment, T3 wrap at NUM_CELLS-1, T4 exactly 2 markers
  across 2*NUM_CELLS ticks, T5 top-bit observability) -- 6/6 PASS at
  both 50T (NUM_CELLS=16384, CTR_W=14) and 200T (131072, 17).
- tb_usb_data_interface.v: existing test 7-8 retargeted from the old
  hardcoded `>=15` / `==15'd16384` invariant to the new parameterized
  one (`==RP_DOPPLER_MEM_ADDR_W` / `==RP_MAX_OUTPUT_BINS*RP_NUM_DOPPLER_BINS`).

Regression: 41/41 PASS (+2 new entries: 50T default + 200T
`+define+SUPPORT_LONG_RANGE`).
2026-04-29 23:01:41 +05:45
Jason 1f307f77a9 cosim: refresh stale baselines (FFT-2048 + chirp realign)
Two stale-baseline events were never captured in earlier commits:

1. The FFT-1024 -> FFT-2048 merge (c668652) updated the testbench and
   gen_mf_cosim_golden.py but left radar_scene.py FFT_SIZE=1024. When
   FFT_SIZE was later bumped to 2048, the input vectors written by
   generate_baseband_samples (bb_mf_test_*.hex, ref_chirp_*.hex) grew
   from 1024 to 2048 samples but were never re-exported.

2. The TX-I matched-filter realignment (5ff5671) changed the ADC chirp
   phase from 2*pi*F_IF*t to 2*pi*(F_IF+F_BASEBAND_LOW)*t. ADC sample
   values shifted from sample ~1336 onward but adc_*.hex was never
   re-exported.

Result: every regression run produced a "dirty" working tree as the
regen reproduced post-merge values that disagreed with the committed
baselines. Two consecutive regen runs are bit-exact identical
(LCG seed=42 + deterministic chirp math) — verified via diff -q on
two output dirs. There is no actual non-determinism; only stale
artifacts.

This commit refreshes all 15 affected files in one shot:
- 6 input hex (adc_*_target.hex, bb_mf_test_*.hex, ref_chirp_*.hex)
- 5 RTL output csv (rtl_*.csv from current RTL)
- 4 compare csv (compare_mf_*.csv = py vs rtl side-by-side)

Verification: full regression 39/39 PASS on the refreshed inputs.
After this commit, regression runs should leave the working tree clean.
2026-04-29 20:33:55 +05:45
Jason 58154a6bf1 fpga: split gpio_dig5/dig7 by fault class (AUDIT-S10)
gpio_dig5 (PD13) previously OR'd six flags — four signal-saturation
classes (AGC, DDC overflow, DDC saturation, MTI saturation) and two
control-fault classes (range-decimator watchdog from F-6.4, CIC->FIR
CDC overrun from F-1.2). The MCU outer-loop AGC reduces RF gain on
PD13 assertion, which is the wrong response to a watchdog or CDC
stall — it just hides the stall behind a quiet receive chain. gpio_dig7
(PD15) was tied 1'b0 as "reserved".

Split:
  gpio_dig5 = signal-saturation only (AGC continues to react correctly)
  gpio_dig7 = control-fault classes

Telemetry: status_words[5][6:5] now exposes the two control-fault
classes in BOTH legacy (FT601) and FT2232H USB variants, with 2-FF
level CDC sync from clk_100m to ft601_clk_in / ft_clk. Bit [7] is
reserved. AUDIT-C12's frame_drop_count at [31:25] is preserved.

50T XDC H12 -> gpio_dig7 pin already assigned (audit AUDIT-C15-era);
no XDC change.

Test: tb/tb_audit_s10_gpio_split.v 17/17 PASS — exercises both the
combinational GPIO split and the CDC status-word packing path.
Regression: 39/39 PASS (was 34/34).
2026-04-29 20:06:52 +05:45
Jason 59f3c82fbb fpga: wire AD9484 PWDN to host opcode 0x32 (AUDIT-S25)
`radar_receiver_final.v:246` had `assign adc_pwdn = 1'b0;` -- the AD9484
PWDN pin was hard-tied LOW with no path for the host or MCU to assert
it. Combined with AUDIT-C13 (CSB hard-tied HIGH on the production board,
no SPI access to the AD9484), the ADC was fully un-recoverable from a
stuck state without dropping main power -- which also drops the
VBAT-backed BKPSRAM persistence (MCU-A4 OCXO warmup, MCU-A7 emergency
flag) and forces a 180 s warmup soak.

Opcode 0x32 was reserved during the AUDIT-C3 fix (commit 24ef5e7) for
exactly this purpose. Wire it through:

  - `radar_system_top.v` adds `reg host_adc_pwdn` next to `host_adc_format`,
    resets to 1'b0 (matches historical hard-tied state -- preserves
    bringup behavior), latches `usb_cmd_value[0]` on opcode 0x32, drives
    the new receiver input port.
  - `radar_receiver_final.v` adds `input wire host_adc_pwdn`, replaces the
    hard-coded `assign adc_pwdn = 1'b0` with `assign adc_pwdn = host_adc_pwdn`.
  - No CDC: `host_adc_pwdn` is a stable single-bit level driven from the
    clk_100m register straight to the I/O pad. AD9484 PWDN is asynchronous
    w.r.t. the ADC clock; the chip re-acquires its DLL on PWDN deassert.

XDC pin assignments were already in place from AUDIT-C15 (50T:T5,
200T:P20, both LVCMOS25 driving the AD9484 PWDN net via the R36/R37
divider on the Main Board).

Verification:
  - new tb/tb_adc_pwdn_opcode.v, 15/15 PASS:
      T1 reset -> host_adc_pwdn=0, adc_pwdn pin=0 (ADC powered up)
      T2 opcode 0x32 val=1 -> host_adc_pwdn=1, pin=1 (PWDN asserted)
      T3 opcode 0x32 val=0 -> cleared
      T4 only bit[0] consumed (upper bits ignored)
      T5 unrelated opcodes (0x33, 0x01) don't disturb host_adc_pwdn
      T6 cmd_valid_100m gating works
  - Quick regression 33/33 PASS (was 32/32; +1 new test, 0 regressions)
  - Lint: 0 errors
2026-04-29 19:37:37 +05:45
Jason ea2615ef84 doppler: gate S_IDLE→S_ACCUMULATE on frame_start_pulse (AUDIT-S3)
Pre-fix S_IDLE had two independent if-branches: one for frame_start_pulse
(resets pointers) and one for data_valid (transitions to S_ACCUMULATE).
A data_valid arriving before frame_start_pulse would advance the FSM with
whatever pointers happened to be live, and the BRAM write block would write
the sample into mem_write_addr = (write_chirp_index*RANGE_BINS) + 0.

In current operation the race is benign — end-of-S_ACCUMULATE always zeros
write_chirp_index/write_range_bin (line 287-288) and the MF pipeline latency
(~165 µs) is millions of cycles longer than the frame_start CDC latency
(~50 ns), so frame_start always arrives first. But the FSM relies on an
undocumented system-level invariant; a future code path that leaves
pointers stale on entry to S_IDLE would silently corrupt the first sample.

Fix: add a `frame_armed` register set when frame_start_pulse arrives in
S_IDLE, cleared on transition to S_ACCUMULATE. Both the FSM transition and
the BRAM write block gate on `(frame_start_pulse || frame_armed)`. The OR
admits the same-cycle case where both arrive together (write to addr 0
still resolves correctly because both blocks use the same gate).

Verification: tb_doppler_frame_start_gate 21/21 PASS, quick regression
32/32 PASS (was 31/31; +1 new test, 0 regressions). tb_doppler_realdata
(full FFT pipeline) still passes — gate transparent to normal operation.
2026-04-29 18:36:31 +05:45
Jason 53c7f416a7 cfar_ca: reset detect_count per frame (AUDIT-C6)
Bug: 16-bit detect_count was reset only on power-on; increments at three
sites (ST_IDLE/ST_BUFFER simple-threshold paths and ST_CFAR_CMP) accumulate
across frames. At 178 fps with even 2-3 average detections per frame the
counter wraps in 100-180 seconds, breaking any rate-based host telemetry
or health check that reads it.

Fix: add `detect_count <= 16'd0` in ST_DONE so the counter represents
"detections this frame" instead of cumulative-since-boot. Updated $display
wording from "total detections" to "frame detections".

T13 flipped from "count keeps growing" to "identical-scene frames produce
identical counts" (the actual contract a per-frame counter must satisfy).
TB snapshots detect_count during ST_DONE because cfar_busy only goes low
on ST_IDLE entry — after the reset has fired.

Verification: tb_cfar_ca 24/24 PASS, quick regression 31/31 PASS.

Note: detect_count output port is now "live" (accumulates during frame,
0 between frames). Audit confirmed no current host telemetry consumes
this port. If future host code needs a stable last-frame total, add a
detect_count_last_frame snapshot register then.
2026-04-29 18:09:28 +05:45
Jason e67368d621 ft2232h: add frame drop counter (AUDIT-C12) + cfar RMW cadence guard (AUDIT-S22)
AUDIT-C12: usb_data_interface_ft2232h had a misleading single-buffer comment
that overstated the timing slack and referenced a frame_ack_toggle CDC that
was never implemented. Re-verified actual numbers: at 178 fps the slack is
1.14 ms (20%), not "much shorter than gap". No data corruption today (write
order matches read order, addresses don't collide), but frame_complete
firing while WR_FSM is still draining the previous frame causes silent
frame drops via the missed frame_ready_toggle edge.

Fix is instrumentation, not architectural rework: add wr_done_toggle
(ft_clk -> clk CDC) on WR_DONE -> WR_IDLE, track frame_pending in clk
domain, count drops in 7-bit saturating frame_drop_count, surface in
unused upper 7 bits of status_words[5]. Host now has visibility into the
failure mode if margin ever shrinks (faster frame rate or USB bandwidth
shortfall). Replaced misleading comment with corrected timing breakdown.

AUDIT-S22: cfar_ca emits one detection per 3 cycles (THR/MUL/CMP); the
detection RMW takes 3 cycles. Match by construction today, fragile against
any CFAR speedup. Added a header comment in cfar_ca.v documenting the
dependency, and a SIMULATION-only assertion in usb_data_interface_ft2232h.v
that fires [ASSERT FAIL] AUDIT-S22 if cfar_valid arrives while RMW busy.
Catches silent-drop regressions in the test suite.

Verification: new tb_ft2232h_frame_drop.v with 5 scenarios (no drops /
stalled drops / multi-drop / recovery / saturation at 127) - 10/10 PASS.
Quick regression 31/31 PASS (was 30/30; +1 new test, 0 regressions).
2026-04-29 17:51:30 +05:45
Jason 0c82de54a2 fft_engine_axi_bridge: respect axi_din_tready with 1-deep skid buffer
Bug: bridge advanced in_count and asserted tlast on din_valid alone,
ignoring the IP's tready handshake. With LogiCORE FFT v9.1 in
nonrealtime throttle mode (per .xci), tready can deassert briefly
during BFP normalization or pipeline events, silently dropping input
samples and shifting tlast off-by-N.

Fix: add 1-deep skid buffer + AXI-correct handshake. Phase 1 drains
the active beat when the IP accepts it (and shifts skid up); Phase 2
loads new upstream samples respecting post-handshake slot availability.
Track accept_count separately from in_count to drive the S_FEED->S_DRAIN
transition on the Nth accepted beat. Sustained 2+ cycle backpressure
exhausts the skid and sets overflow_sticky for debug visibility.

Audit cross-refs (AUDIT-C10):
- "tready ignored" - CONFIRMED, fixed here
- "SCALE_SCH unset" - REFUTED (BFP mode uses tuser, not cfg_tdata)
- "output ordering not configured" - REFUTED (.xci natural_order)

Verification: new tb_fft_engine_axi_bridge.v with stub xfft_2048
exercises 4 backpressure patterns (none / dip-at-3 / dip-at-100 /
3-cycle sustained). Quick regression 30/30 PASS.
2026-04-29 17:24:21 +05:45
Jason 24ef5e7251 fix(fpga): C-3 — parameterize DDC ADC sign-conversion via host opcode 0x33
The DDC hard-coded an offset-binary->2C subtract on the AD9484 path. The
chip's output format is selected by the SCLK/DFS strap (jumper SJ1 on
RADAR_Main_Board.sch), and CSB is hard-tied HIGH so SPI cannot be used
to confirm or change it from firmware. If the board is assembled with
SJ1 on pins 2-3 (two's-complement), the existing RTL silently mis-
converts every sample.

Add a 2-bit adc_format input to ddc_400m_enhanced (2-FF synchronized
clk_100m -> clk_400m, ASYNC_REG attribute), drive it from a new top-
level register host_adc_format written by host opcode 0x33, and wire
it through radar_receiver_final. Default 2'b00 matches the SJ1 default
strap (offset-binary) and preserves pre-patch behavior. Opcode 0x32 is
intentionally left unused; reserved for the future S-25 fix
(host-driven adc_pwdn).

Tests: tb/tb_ddc_400m.v Test Group 5 — 7 new assertions covering
offset-binary at {0x80, 0x00, 0xFF}, two's-complement at
{0x00, 0x80, 0x7F}, and reserved 2'b10 fallback. 14/14 PASS.

Refs: AUDIT-C3 (DDC offset-binary hardcoded).
Schematic ref: RADAR_Main_Board.sch:46719 (CSB on +1V8_CLOCK_F),
:46845 (SCLK/DFS via SJ1).
2026-04-29 14:18:25 +05:45
Jason 4f0b82de6e test(fpga): receiver-integration — fix tb wiring + skip-guard XSim-only checks
tb_radar_receiver_final had three pre-existing issues that all surfaced as
fails in regression (32 passed, 2 failed before; 34 passed, 0 after):

1. host_range_mode was undriven (floating 2'bzz); rmc log confirmed
   "Auto-scan starting, range_mode=z". Add explicit 2'b01 (long-range
   dual-chirp) for the test scenario.

2. DDC_MAX_ENERGY threshold (2^56) was sized for an unspecified earlier
   stimulus; the test feeds a deliberately-loud 120 MHz sawtooth that
   produces ~1.27e17 energy over 2M samples. Raised to 2^60 (~10x
   observed) so B1b catches true overflow without false-firing.

3. The 9 doppler-frame-dependent checks (S4-S9, G1, B2a, B3, B4) need
   ~108 ms simulated time to fill a 32-chirp Doppler frame because the
   in-house fft_engine takes ~340 K cycles per multi-segment chirp
   (RX-NEW-3, commit 5c8cc8c). Iverilog can't elaborate the Xilinx FFT IP
   that would make this tractable. Guard those checks behind
   `ifdef FFT_USE_XILINX_IP` so iverilog cleanly SKIPs them with an
   explanatory line; XSim with the IP runs them normally.

Also tightens run_regression.sh's pass/fail regex from
^\[(PASS|FAIL)([^]]*)\] to ^\[(PASS|FAIL)( [0-9]+)?\] so informational
tags like [FAIL-INFO] (used to document the known RX-NEW-1 fft_engine
bin-shift in tb_matched_filter_processing_chain.v) no longer false-fire
as real failures. The Matched Filter Chain test goes from FAIL (40 pass,
2 false-fails) to PASS (40 checks).

Regression: 34 passed, 0 failed.
2026-04-29 11:41:40 +05:45
Jason 5ff5671fe2 fix(fpga): TX-I — align matched-filter reference with actual post-DDC band
The DAC short/long chirp LUTs are 10..30 MHz upchirps (Hilbert-confirmed).
With TX_LO=10.500 GHz, RX_LO=10.380 GHz (adf4382a_manager.h) and the
120 MHz DDC NCO (ddc_400m.v), high-side mixing places the post-DDC echo
at 10..30 MHz baseband. The matched-filter reference (gen_chirp_mem.py)
was generating 0..20 MHz, implicitly assuming the chirp's low edge mixed
to DC. This caused a 10 MHz spectral offset and ~5 dB matched-filter loss.

Adds F_BASEBAND_LOW=10e6 in both gen_chirp_mem.py and radar_scene.py,
with phase formula 2*pi*F_BASEBAND_LOW*t + pi*rate*t^2 in all chirp
generators. Regenerates the 6 .mem files. Adds analyze_short_chirp_mismatch.py
for the Hilbert-based diagnosis. Fixes the misleading "30MHz to 10MHz"
comment in plfm_chirp_controller.v and adds an end-to-end frequency plan
in the LUT header.

Sideband orientation (high-side at both mixers) is the conventional choice
and consistent with antenna match (10.25..10.75 GHz, 8x16 patch designed
at 10.5 GHz). Loopback capture would settle definitively; if either mixer
is low-side the F_BASEBAND_LOW sign flips and/or chirp direction reverses.
2026-04-29 11:41:19 +05:45
Jason b7ac2de1a4 chore: delete dead latency_buffer; doc cleanup for two stale comments
latency_buffer.v has had zero non-tb instantiations since RX-B (2026-04-23)
replaced its hookup in radar_receiver_final with a 1-FF alignment register.
The module was being kept "for potential future use" — exactly the kind of
dead weight the codebase does not need. Deleted, along with all build /
test infrastructure that dragged it along:

  - 9_Firmware/9_2_FPGA/latency_buffer.v
  - 9_Firmware/9_2_FPGA/tb/tb_latency_buffer.v
  - run_regression.sh: removed from RTL_FILES and RECEIVER_RTL
  - scripts/200t/build_200t.tcl: removed from synthesis source list
  - tb/tb_system_e2e.v: removed from header compile-string example
  - tb/cosim/validate_mem_files.py: deleted test_latency_buffer() (~75 lines),
    its call site, and the corresponding entry in the module docstring

Historical RX-B comments referencing latency_buffer in radar_receiver_final.v,
tb_rxb_fullchain_latency.v, and tb_rxb_latency_measure.v are kept — they
explain WHY the module was removed, which is still useful design archaeology.

Two doc-only housekeeping touches bundled in:

  - plfm_chirp_controller.v: replaced two empty "CRITICAL FIX: Generate
    valid signal" labels at LONG_CHIRP and SHORT_CHIRP with one shared
    chirp_valid policy comment block above LONG_CHIRP that explains the
    actual rationale (downstream FIFO underrun on trailing samples).

  - v7/models.py: replaced the "range_resolution and velocity_resolution
    should be calibrated" docstring (sounded like an open TODO but was a
    documented placeholder) with a clear pointer to the GUI-C3 fix in
    workers.py:RadarDataWorker so future readers know the live path
    derives correct values from WaveformConfig.

FPGA quick regression unchanged: 28/29 (1 fail is the unrelated iverilog/
Xilinx-IP RX-NEW-3 gap). GUI suite 180/180. Ruff clean.
2026-04-28 12:52:13 +05:45
Jason 0b8b933e27 cleanup(fpga): RX-A1 — drop dead chirp_counter port from MF chain
matched_filter_processing_chain declared `input wire [5:0] chirp_counter`
but never read it inside the module. matched_filter_multi_segment passed
its own chirp_counter through to that dead port.

Removed the port from the chain and the corresponding hookup at the
multi_segment instantiation site. Five testbenches also referenced the
port (tb_mf_cosim, tb_matched_filter_processing_chain, tb_rxb_latency
_measure plus the four MF cosim variants that share tb_mf_cosim) — the
reg/connection/init lines were dropped, and the now-stale "Test Group 8:
Chirp Counter Passthrough" was repurposed as a port-removal smoke test
that confirms the chain still produces FFT_SIZE outputs without that
input.

multi_segment.chirp_counter input remains on the port list (it could
plausibly be wired to per-chirp logic in the future); it is now formally
unused but iverilog/Vivado do not flag unused module inputs.

Quick regression: 28/29 PASS (same as baseline; the 1 fail is the known
iverilog/Xilinx-IP RX-NEW-3 gap unchanged by this commit).
2026-04-27 14:06:55 +05:45
Jason ca2b6e527d fix(fpga): TX-G — surface chirps_mismatch_error to host status
`chirps_mismatch_error` was set in radar_system_top when the host
requested chirps_per_elev != Doppler FFT size, but never wired into the
USB status response — a latent silent failure.

Wired the flag through both USB interfaces (FT601 + FT2232H) into bit
[10] of status word 4 (was reserved). GUI parser exposes it as
StatusResponse.chirps_mismatch.

- usb_data_interface*.v: new status_chirps_mismatch input, packed at [10]
- radar_system_top.v: connect chirps_mismatch_error to both USB instances
- radar_protocol.py + test_GUI_V65_Tk.py: parse new bit, +1 round-trip test
- tb_usb_data_interface.v: drive the new port, update word-4 expectation

Tests: GUI 92/92 (was 91), MCU 75/75, USB TB 91/91, ruff clean repo-wide.
The 2 remaining FPGA regression failures (Receiver Integration, MF Chain)
are the pre-existing iverilog-can't-link-Xilinx-IP issue tracked
separately as the open RX-NEW-3 follow-up.
2026-04-24 11:06:26 +05:45
Jason 89dc9156c7 fix(fpga): RX-F — MTI exits mute on chirp boundary, not just last bin
mti_canceller previously armed has_previous and refreshed
prev_chirp_was_long only when range_bin_d1 == NUM_RANGE_BINS - 1.
range_bin_decimator can early-terminate a chirp before reaching the
last bin (overflow guard at range_bin_decimator.v:306, watchdog at
:314), so on every such chirp MTI never armed and stayed muted forever
on every subsequent chirp until reset.

Detect chirp boundary internally using bin-0 arrival after at least
one non-zero bin in the prior chirp. effective_has_previous lifts
has_previous=1 the cycle chirp_boundary fires so the new chirp's
bin-0 is subtracted (read-before-write on prev[0] correctly returns
the previous chirp's bin-0). prev_chirp_was_long now updates on every
range_valid_d1 (no-op within a chirp; OLD value still visible at the
chirp_boundary cycle for the waveform_changed compare). Pass-through
clears saw_nonzero_bin_in_chirp so the first MTI-enabled chirp after
a pass-through run is correctly muted.

No port changes. tb_mti_canceller T13 added: feed a 32/64-bin partial
chirp followed by a full chirp, verify the second chirp is NOT muted
(would fail without the fix). MTI Canceller goes from 40 -> 43 checks,
all passing. Local regression: 32/34 PASS (same as baseline; the two
failing tests are pre-existing RX-NEW-3 FFT throughput).
2026-04-23 19:58:08 +05:45
Jason 5c8cc8c96a feat(fpga): swap matched-filter chain to Xilinx LogiCORE FFT v9.1 IP
Replaces the in-house iterative fft_engine.v in the matched-filter chain
with the Pipelined Streaming Xilinx FFT IP, closing RX-NEW-3 (FFT chain
~11x too slow vs PRI budget).

Components:
  * ip/xfft_2048_ip/xfft_2048_ip.xci — committed IP definition
    (16-bit fixed point, BFP scaling, convergent rounding, natural order,
    pipelined-streaming, BRAM data/reorder/phase factors). Vivado
    regenerates .dcp / sim-netlist from this on each build.
  * scripts/50t/gen_xfft_2048_ip.tcl — IP-Catalog generation script
  * scripts/50t/run_xfft_xsim.sh — XSim batch runner for tb_xfft_2048_xsim
  * xfft_2048.v — AXI-Stream wrapper. FFT_USE_XILINX_IP define routes to
    real LogiCORE for synth/XSim; falls back to fft_engine batched
    one-shot for iverilog (unit coverage only).
  * fft_engine_axi_bridge.v — exposes legacy fft_engine port surface on
    top of the xfft_2048 AXI wrapper, so the chain swap is a 1-line
    module-name change.
  * matched_filter_processing_chain.v — fft_engine -> fft_engine_axi_bridge
  * scripts/50t/build_50t.tcl — read_ip + generate_target + synth_ip;
    adds FFT_USE_XILINX_IP to verilog defines.
  * tb/tb_xfft_2048_xsim.v — XSim verification (DC, impulse, tone bin 128).
    All 5 assertions PASS on remote with the real IP; tuser=0x0a (BLK_EXP=10)
    confirms BFP scaling working.

Local iverilog regression: 32/34 PASS — identical to baseline. Same two
RX-NEW-3 failures (Receiver Integration, Matched Filter Chain) — these
only resolve in remote XSim with the real IP, since iverilog uses the
fft_engine fallback inside xfft_2048 (~150K cycles/pass, not the
~2200-cycle Pipelined Streaming throughput). MF cosim 4/4 PASS confirms
bridge bit-exact in fallback mode.

Pending: remote XSim of tb_radar_receiver_final to demonstrate Doppler
frames produced within PRI budget; remote synth to confirm DSP/timing
post-IP.
2026-04-23 12:39:33 +05:45
Jason bf39941074 fix(fpga): RX-NEW-2 — replace impossible peak/mean assertions with flatness bounds
The Group 3 (tone autocorrelation), Group 10 (golden DC autocorr), and
Group 11 (golden tone autocorr) tests asserted cap_max_abs > mean_abs * 2,
which is mathematically impossible for those stimuli regardless of FFT
precision:

  - DC autocorrelation produces a constant-magnitude time-domain output
    (peak/mean ≡ 1.0 by definition).
  - Single-tone autocorrelation produces a constant-magnitude rotating
    phasor; |I|+|Q| envelope varies in [|X|^2, sqrt(2)*|X|^2], so
    peak/mean is bounded by ~1.41x.

Empirical RTL output ratios from this regression: DC=1.07x, Tone5=1.18x,
Chirp=3.14x, Impulse=2015x — confirming theory and confirming the FFT
engine is correct for narrow-spectrum inputs.

Replace each ">2x" check with mean>0 && peak<=mean*2 (flatness bound).
Still catches flat-zero output (mean=0) but admits the correct constant-
magnitude result.

Matched Filter Chain regression: 5 failures -> 2 failures.
2026-04-23 07:39:16 +05:45
Jason f1f69ca623 ci(fpga): wire RX-B latency tests; fix downstream compile after inline-FFT removal
- run_regression.sh: add frequency_matched_filter.v to PROD_RTL and RECEIVER_RTL
  compile groups (was implicitly required after inline behavioural FFT in
  matched_filter_processing_chain.v was removed); empty EXTRA_RTL with set -u
  guards; bump Matched Filter Chain timeout to 600s.
- run_regression.sh: add two PHASE 3 tests — tb_rxb_latency_measure (chain
  pipeline depth) and tb_rxb_fullchain_latency (multi-segment + chain).
- radar_receiver_final.v: replace dangling delayed_ref_i/q references (left
  over from latency_buffer removal) with ref_chirp_real/imag.
- tb/tb_radar_receiver_final.v: chain-state debug uses production
  collect_count/out_count signals instead of the deleted SIMULATION-only
  fwd_in_count.
- tb/tb_rxb_latency_measure.v: add explicit [PASS]/[FAIL] markers around the
  2007..2107 cycle expected-latency window.
2026-04-23 06:34:05 +05:45
Jason 9d1eb4b11c fix(radar): RX chain corrections, GUI bin alignment, MCU boot ordering
FPGA — RX chain
  matched_filter_multi_segment.v: drop the gratuitous /4 scaling on
    DDC sign-extended input (was ddc_i[17:2] + ddc_i[1]); use
    ddc_i[15:0] directly. fft_engine has INTERNAL_W=32 with
    saturating 16-bit output, so full 16-bit input is safe. Restores
    ~12 dB of MF input dynamic range.
  radar_receiver_final.v: remove latency_buffer (count-N-pulses-then-
    prime FIFO that left frame 1 with all-zero ref). Replaced with
    a single-FF alignment register on ref_i/ref_q that matches the
    1-FF stage multi_segment ST_PROCESSING uses on adc_data.
    Verified by tb/tb_rxb_fullchain_latency.v — autocorrelation peak
    at bin 0 with peak/mean ~88x.
  doppler_processor.v / mti_canceller.v / cfar_ca.v /
    range_bin_decimator.v / radar_receiver_final.v / radar_system_top.v
    / usb_data_interface_ft2232h.v: switch port and parameter widths
    from RP_NUM_RANGE_BINS / RP_RANGE_BIN_BITS (always 512 / 9-bit)
    to RP_MAX_OUTPUT_BINS / RP_RANGE_BIN_WIDTH_MAX (auto-scales:
    50T 512 / 9-bit, 200T 4096 / 12-bit). Unblocks 200T 20 km mode
    at the RX module boundary; USB wire-protocol extension still
    pending.
  radar_receiver_final.v: doppler_frame_done_prev reset value 0 -> 1
    to prevent false done pulse on cycle 1 when level signal is
    HIGH at reset.
  matched_filter_processing_chain.v: delete the broken `ifdef
    SIMULATION inline behavioural FFT (482 lines removed). It
    produced wrong-bin peaks and 100-1000x weak magnitudes. Chain
    now uses production fft_engine.v + frequency_matched_filter.v
    in both iverilog and Vivado. Iverilog tests are ~38x slower per
    chain pass but produce correct results. Misleading "OK with
    Xilinx IP" comments at three test sites updated since the FFT
    is in-house, not an IP placeholder.

FPGA — testbenches
  tb/tb_rxb_latency_measure.v (new): measures chain internal pipeline
    depth (~2057 cycles, chirp-agnostic).
  tb/tb_rxb_fullchain_latency.v (new): full-chain autocorrelation
    verification — drives ddc with the same chirp samples the loader
    serves as ref, finds peak position and peak/mean.
  tb/tb_matched_filter_processing_chain.v: wait timeouts bumped
    50000 -> 500000 cycles to accommodate production FFT pipeline.

MCU
  main.cpp checkSystemHealthStatus: latch system_emergency_state on
    the error_count > 10 path so the SAFE-MODE blink loop in main()
    actually engages (was bypassed because predicate was false).
  main.cpp: move FPGA reset BEFORE the if(PowerAmplifier) block so
    adar_tr_x is driven LOW (RX commanded externally) before PA Vdd
    reaches 22 V. Old reset block at the original location removed.
  main.cpp MX_GPIO_Init: add GPIO_PIN_12 (FPGA reset) to the
    explicit WritePin(LOW) list so the safe initial state is no
    longer implicit.
  main.cpp checkSystemHealth: rate-limit ADAR1000
    verifyDeviceCommunication (HAL_Delay 1ms x 4 devices = 4 ms
    blocking SPI burst per main-loop iteration) from every-loop to
    every 2 s. readTemperature stays per-loop so over-temp
    detection latency is unchanged.
  USBHandler.cpp processSettingsData: dispatch threshold bumped
    74 -> 82 (matches parser minimum); buffer drained after parse
    attempt (slide remaining bytes left) so a false END find no
    longer sticks the buffer until 256-byte overflow.

GUI
  radar_protocol.py: NUM_RANGE_BINS 64 -> 512 (matches FPGA
    RP_NUM_RANGE_BINS); NUM_CELLS 2048 -> 16384.
  radar_protocol.py _ingest_sample: honor FPGA frame_start bit for
    resync after a USB drop; capture range_profile[rbin] once per
    range bin at dbin == 0 (FPGA emits the same range_i/range_q for
    all 32 Doppler cells of a given range bin; previous accumulator
    inflated the profile 32x).
  v7/models.py RadarSettings: range_resolution 24 -> 6 m (matches
    c/(2*100MHz)*4); max_distance and coverage_radius 1536 -> 3072 m;
    map_size 2000 -> 4000.
  v7/models.py WaveformConfig: n_range_bins 64 -> 512, fft_size
    1024 -> 2048, decimation_factor 16 -> 4.
  GUI_V65_Tk.py: _RANGE_PER_BIN math and stale "~24 m / ~1536 m"
    comments updated.
  test_v7.py: assertion values updated to match new defaults.

Tests
  test_ddc_cosim_fuzz.py: remove unused os/tempfile imports, wrap
    three long lines for ruff E501 compliance.
2026-04-23 05:56:52 +05:45
Jason 27c9c22ad2 test(fpga): regression coverage for C-3 and USB NUM_CELLS bugs
Two bugs fixed recently had no tests that would have failed before the
fix. Add direct regressions so either cannot silently return:

1. tb_chirp_controller Group 3b (multi-frame, C-3): run a second full
   frame back-to-back after DONE and assert chirp_counter returns to 0,
   frame 2 reaches GUARD_TIME after exactly CHIRP_MAX/2 long chirps,
   and frame 2 reaches DONE. Before the fix, chirp_counter held at
   CHIRP_MAX after frame 1, the LONG_LISTEN -> GUARD guard (=CHIRP_MAX/2-1)
   never matched, and frame 2 ran extra chirps until the 6-bit counter
   wrapped — these checks fail loudly if that regresses.

2. tb_usb_data_interface frame-sync width + value pins: assert
   $bits(uut.sample_counter) >= 15 and uut.NUM_CELLS == 15'd16384.
   Protects against reintroducing the 12-bit / 2048-cell constants
   that fired 8 false frame-start markers per real 512 x 32 frame.

Regression: 32/32 PASS; USB TB 89 -> 91 checks.
2026-04-22 19:44:25 +05:45
Jason 3d0ee50999 fix(fpga): reset chirp_counter at DONE; source CHIRP_MAX from radar_params
C-3: plfm_chirp_controller_enhanced never reset chirp_counter when the
frame completed. Counter sat at CHIRP_MAX after frame 1, so the
LONG_LISTEN -> GUARD transition guard (== CHIRP_MAX/2-1) never matched
correctly on subsequent frames and frame 2+ ran extra chirps until the
6-bit counter wrapped. Reset chirp_counter in the DONE state.

S-2: Replace hardcoded CHIRP_MAX = 32 with RP_CHIRPS_PER_FRAME from
radar_params.vh so the TX FSM tracks the single source of truth.

S-1: Correct misleading labels in tb_system_e2e G14.1-G14.3. Per
radar_params.vh the range_mode encoding is 2'b00 = 3 km, 2'b01 =
long-range, 2'b10/2'b11 = reserved. The TB strings previously called
2'b01 "short" and 2'b10 "long", which is inverted and inconsistent
with the RTL comments in radar_mode_controller.v.

Regression: 32/32 PASS.
2026-04-22 19:34:09 +05:45
Jason 21aaa5ac33 fix(fpga): correct USB frame-sync counter for 512x32 cell grid
usb_data_interface.v NUM_CELLS was still 12'd2048 (64 range x 32 doppler)
from the pre-2048-FFT architecture. With 512 range bins x 32 Doppler, the
12-bit counter wrapped every 2048 packets and the host received 8 false
frame-start markers per real frame via the sample_counter==0 bit packed
into the detection byte. Widen counter to 15 bits and set NUM_CELLS to
16384. Sister file usb_data_interface_ft2232h.v was already correct.

Remove three stale testbenches hardcoded to the old 1024-pt / 64-bin
architecture (tb_mf_chain_synth, tb_fullchain_mti_cfar_realdata,
tb_range_fft_realdata). Equivalent current-architecture coverage already
exists in tb_matched_filter_processing_chain, tb_fullchain_realdata,
tb_fft_engine, tb_multiseg_cosim, and tb_mf_cosim.
2026-04-22 15:44:48 +05:45
Jason f39a78cb1e chore(fpga): untrack TB-generated CSV, ignore a.out
rx_final_doppler_out.csv is written by tb_radar_receiver_final.v on
every run via $fopen — it is a test-run artifact, not an oracle. It
was mistakenly tracked in an earlier commit, causing unnecessary
churn on every sim. Remove from the index and ignore going forward.

Also ignore stray a.out from iverilog one-shot compiles.

Golden references (.hex, .mem, doppler_golden_py_*.csv) remain
tracked — they are load-bearing oracles used by MF / Doppler /
receiver cosim testbenches.
2026-04-22 13:36:03 +05:45
Jason 8865e9a0ef fix(fpga): pre-bringup RTL hardening + test-suite hardening
RTL (P0 pre-bringup findings R-1/R-2/R-3/R-5/R-6):

- mti_canceller: add use_long_chirp input and waveform-boundary mute
  so the long->short transition in mode 01 no longer subtracts across
  heterogeneous waveforms (R-1). Prev buffer is overwritten in-flight
  at the boundary so the next same-waveform chirp subtracts cleanly.
- ad9484_interface_400m: 2FF sync of mmcm_locked into the 400 MHz
  domain before gating reset_n_gated (R-6).
- cic_decimator_4x_enhanced: correct max_fanout narrative (R-3).
- ad9484_interface_400m: strip stale pblock comment, note 3.0 ns
  max_delay instead (R-2).
- mti_canceller / doppler_processor: 200T-20km WARNING banners
  flagging the broken 4096-bin path (R-5). 9-bit BRAM address aliases
  silently until rewritten.
- adc_clk_mmcm.xdc: relax set_max_delay from 2.700 -> 3.000 ns,
  closes WNS with headroom on 50T build.
- radar_receiver_final: wire use_long_chirp into mti_inst.

Architecture-bump finalization (2048-pt range FFT, 512 range bins,
32 Doppler bins -> 16384 output cells per frame):

- tb/cosim/radar_scene.py: FFT_SIZE 1024 -> 2048, RANGE_BINS 64 -> 512.
- tb/gen_mf_golden_ref.py: N 1024 -> 2048.
- Regenerate all affected hex goldens (MF cases 1-4, Doppler inputs
  + py goldens, receiver integration golden_doppler.mem 2048 -> 16384).
- tb_radar_receiver_final: widen range_bin_out 6 -> 9 bits, bump
  GOLDEN_ENTRIES 2048 -> 16384, expand bitmaps/arrays to 512 bins,
  update all check messages and thresholds.
- tb_mti_canceller, tb_fullchain_mti_cfar_realdata: tie/pass
  use_long_chirp so compile still works after RTL port add.

Test-suite hardening (coverage audit findings):

- tb_mti_canceller T12: 10 new assertions exercising R-1 waveform-
  boundary mute across a long/long/short/short/long sequence. Catches
  a regression that re-enables subtraction across the boundary.
- tb_fir_lowpass: replace tautological check(1'b1, ...) on coefficient
  symmetry with a real hierarchical check coeff[k]===coeff[31-k];
  replace always-pass overflow check with a well-driven (not X/Z)
  assertion on filter_overflow.
- tb_matched_filter_processing_chain: replace three always-pass peak-
  bin placeholders with peak-to-mean-|out| > 2x ratio checks (catches
  flat/zero output that the old tautologies silently accepted).
- tb_cdc_modules M2: replace always-pass narrow-pulse check with a
  well-defined-output assertion on the synchronizer.
- tb_nco_400m: replace always-pass freq-switch check with a swing +
  no-X assertion across 200 post-switch samples.
- tb_system_e2e G12.1: replace check(1, ...) with test_num > 20 so
  it catches a stalled TB that skipped prior groups.
- tb_multiseg_cosim TEST 4: replace always-pass placeholder with a
  bitmap that asserts segment_request visited all 4 values.
- tb_mf_chain_synth and tb_fullchain_mti_cfar_realdata: add DEPRECATED
  headers plus \$fatal guards (ifndef ALLOW_STALE_*) so they cannot
  be silently re-enabled in CI with stale 1024-bin goldens against
  current 2048-pt RTL.

Regression: 32 passed, 0 failed. MTI TB grew 30 -> 39 checks;
receiver integration grew 17 -> 18 checks with 16384/16384 golden
match at tolerance +/- 2 LSB.
2026-04-22 13:23:38 +05:45
Jason c668652ba8 merge(wave3/tier2): port testbenches and cosim goldens for fft-2048
Regression goes from 21/32 -> 27/32 passing.

TB files updated from feat/fft-2048-upgrade (FFT_SIZE=2048 / 512 range
bins / Manhattan magnitude / 2-segment matched filter):
  - tb/tb_mf_cosim.v            (range_profile_{i,q} port names)
  - tb/tb_matched_filter_processing_chain.v  (long_chirp port names)
  - tb/tb_range_bin_decimator.v (new 2048->512 DUT)
  - tb/tb_radar_mode_controller.v (XOR edge detector)
  - tb/tb_doppler_cosim.v       (2048-deep inputs)
  - tb/tb_multiseg_cosim.v
  - tb/tb_mf_chain_synth.v

Cosim infrastructure regenerated with FFT_SIZE=2048:
  - tb/cosim/gen_mf_cosim_golden.py
  - tb/cosim/gen_doppler_golden.py
  - tb/cosim/compare_mf.py, compare_doppler.py
  - tb/cosim/fpga_model.py
  - All mf_* and doppler_* goldens/inputs regenerated

Deliberately NOT taken:
  - tb/tb_radar_receiver_final.v — kept p0's version because the merged
    radar_receiver_final requires tx_frame_start + adc_or_p/n inputs
    that fft's TB does not drive. Its 3 failures (G1 golden mismatch,
    B3/B5 hardcoded 64-bin limits) are tracked as known issues; TB
    needs a 64->512 bin rewrite + golden regen against merged RTL.

Known remaining failures (5/32):
  - Doppler Co-Sim x3: python compare mismatch — goldens generated
    against fft's reset/DDC behavior; merged RTL uses p0's reset
    strategy. Needs golden regen against merged RTL.
  - Receiver Integration: TB has stale 64-bin localparams/widths.
  - Matched Filter Chain: 3/40 "peak magnitude > 0" checks fail on
    behavioral-FFT cases. Pre-existing on fft branch (known brittle).
2026-04-21 03:04:52 +05:45
Jason 60e49c7da6 feat(fpga): integrate 2048-pt FFT upgrade — non-conflicting RTL (wave 1/3)
File-scoped cherry-pick from feat/fft-2048-upgrade (e9705e4) for modules
that only the fft branch modified:

  RTL:
    cfar_ca.v                        512-row CFAR
    chirp_memory_loader_param.v      2-segment × 2048-sample loader
    doppler_processor.v              16384-deep doppler memory
    fft_engine.v                     2048-pt FFT
    matched_filter_multi_segment.v   2-seg overlap-save, BRAM overlap_cache
    matched_filter_processing_chain.v
    radar_mode_controller.v          XOR edge detector
    radar_params.vh                  (new) single source of truth
    range_bin_decimator.v            2048 -> 512 output bins
    rx_gain_control.v

  Memory:
    fft_twiddle_2048.mem             (new) 2048-pt FFT twiddles
    long_chirp_seg0_{i,q}.mem        2048-sample seg 0 (was 1024)
    long_chirp_seg1_{i,q}.mem        2048-sample seg 1 (was 1024)
    long_chirp_seg{2,3}_{i,q}.mem    deleted (4-seg -> 2-seg collapse)

  Gen:
    tb/cosim/gen_chirp_mem.py        regen script for mem files above

Waves 2 and 3 follow: manual merge for dual-modified files
(radar_system_top, usb_data_interface_ft2232h, mti_canceller,
radar_receiver_final), and CFAR pipeline from 2401f5f keeping p0's
CIC/DDC reset strategy.
2026-04-21 01:52:32 +05:45
Jason 51740fd6f5 test(fpga): F-3.2 add DDC cosim fuzz runner with seed sweep
A new SCENARIO_FUZZ branch in tb_ddc_cosim.v accepts +hex / +csv / +tag
plusargs so an external runner can pick stimulus and output paths per
iteration. The three path registers are widened to 4 kbit each so long
temp-directory paths (e.g. /private/var/folders/...) do not overflow
the MSB and emerge truncated — a real failure mode caught while writing
this runner.

test_ddc_cosim_fuzz.py is a pytest-driven fuzz harness:
 - Generates a random plausible radar scene per seed (1-4 targets with
   random range/velocity/RCS/phase, random noise level 0.5-6.0 LSB
   stddev) via radar_scene.generate_adc_samples, fully deterministic.
 - Compiles tb_ddc_cosim.v once per session (module-scope fixture),
   then runs vvp per seed.
 - Asserts sample-count bounds consistent with 4x CIC decimation,
   signed-18 range on every baseband I/Q word, and non-zero output
   (catches silent pipeline stalls).
 - Ships with two tiers: test_ddc_fuzz_fast (8 seeds, default CI) and
   test_ddc_fuzz_full (100 seeds, opt-in via -m slow) matching the
   audit ask.

Registers the "slow" marker in pyproject.toml for the 100-seed opt-in.
2026-04-20 15:48:34 +05:45
Jason b588e89f67 test(fpga): F-2.2 adversarial mid-frame reset sweep + F-0.1 TB plumbing
G9B adds a 4-iteration reset sweep on top of the existing e2e harness:
- Reset is injected at four offsets (3/7/12/18 us) into a steady-state
  auto-scan burst, with mixed short/long hold durations (20-120 clk_100m)
  to exercise asynchronous assert paths through the FSM + CDCs.
- Each iteration asserts: system_status drops to 0 during reset,
  new_chirp_frame resumes post-release, and obs_range_valid_count
  advances — proving the full DDC->MF chain recovers, not just the
  transmitter FSM.

The stub and three existing testbenches are updated to drive the new
adc_or_p/n ports tied to 1'b0/1'b1, matching the F-0.1 RTL change.
2026-04-20 15:48:34 +05:45
Jason 2539d46d93 merge: resolve conflicts with develop (supersede by PR #89 / #107)
Three conflicts — all resolved in favor of develop, which has a more
refined version of the same work this branch introduced:

- radar_system_top.v: develop's cleaner USB_MODE=1 comment (same value).
- run_regression.sh: develop's ${SYSTEM_RTL[@]} refactor + added
  USB_MODE=1 test variants.
- tb/radar_system_tb.v: develop's ifdef USB_MODE_1 to dump the correct
  USB instance based on mode.

The 400 MHz reset fan-out fix (nco_400m_enhanced, cic_decimator_4x_enhanced,
ddc_400m) and ADAR1000 channel-indexing fix remain intact on this branch.
2026-04-19 16:28:07 +05:45
Jason d0b3a4c969 fix(fpga): registered reset fan-out at 400 MHz; default USB to FT2232H
Replace direct !reset_n async sense with a registered active-high reset_h
(max_fanout=50) in nco_400m_enhanced, cic_decimator_4x_enhanced, and
ddc_400m.  The prior single-LUT1 / 700+ load net was the root cause of
WNS=-0.626 ns in the 400 MHz clock domain on the xc7a50t build.  Vivado
replicates the constrained register into ≈14 regional copies, each driving
≤50 loads, closing timing at 2.5 ns.

Change radar_system_top default USB_MODE from 0 (FT601) to 1 (FT2232H).
FT601 remains available for the 200T premium board via explicit parameter
override; the 50T production wrapper already hard-codes USB_MODE=1.

Regression: add usb_data_interface_ft2232h.v to PROD_RTL lint list and
both system-top TB compile commands; fix legacy radar_system_tb hierarchical
probe from gen_ft601.usb_inst to gen_ft2232h.usb_inst.

Golden reference files (rtl_bb_dc.csv, rx_final_doppler_out.csv,
golden_doppler.mem) regenerated to reflect the +1-cycle registered-reset
boundary behaviour; Receiver golden-compare passes 18/18 checks.

All 25 regression tests pass (0 failures, 0 skipped).

Co-Authored-By: Claude Sonnet 4.6 <noreply@anthropic.com>
2026-04-18 20:34:52 +05:45
NawfalMotii79 d3476139e3 Merge pull request #89 from NawfalMotii79/feat/ft2232h-default-ft601-option
feat: make FT2232H default USB interface, add FT601 premium option, deprecate GUI V6
2026-04-17 22:21:58 +01:00
Jason ade1497457 Merge pull request #79 from NawfalMotii79/feat/um982-gps-driver
feat: UM982 GPS driver + deferred fixes (STM32-006, STM32-004, FPGA-001)
2026-04-16 13:54:40 +03:00
Jason f393e96d69 feat(fpga): make FT2232H default USB interface, rewrite FT601 write FSM, add clock-loss watchdog
- Set USB_MODE default to 1 (FT2232H) in radar_system_top.v; 200T build
  overrides to USB_MODE=0 via build_200t.tcl generic property
- Rewrite FT601 write FSM: 4-state architecture with 3-word packed data,
  pending-flag gating, and frame sync counter
- Add FT2232H read FSM rd_cmd_complete flag, stream field zeroing, and
  range_data_ready 1-cycle pipeline delay in both USB modules
- Implement clock-loss watchdog: ft_heartbeat toggle + 16-bit timeout
  counter drives ft_clk_lost, feeding ft_effective_reset_n via 2-stage
  ASYNC_REG synchronizer chain
- Fix sample_counter reset literal width (11'd0 -> 12'd0)
- Add FT2232H I/O timing constraints to 50T XDC; fix dac_clk comments
- Document vestigial ft601_txe_n/rxf_n ports (needed for 200T XDC)
- Tie off AGC ports on TE0713 dev wrapper
- Rewrite tb_usb_data_interface.v for new 4-state FSM (89 checks)
- Add USB_MODE=1 regression runs; remove dead CHECK 5/6 loop
- Update diag_log.h USB interface comment
2026-04-16 16:18:52 +05:45
Jason 15a9cde274 review(cosim): fix stale comment and wrong docstring derivation
golden_reference.py: update comment from 'Simplified' to 'Exact' to
match shaun0927's corrected formula.

fpga_model.py: fix adc_to_signed docstring that incorrectly derived
0x7F80 instead of 0xFF00. Verilog '/' binds tighter than '-', so
{1'b0,8'hFF,9'b0}/2 = 0x1FE00/2 = 0xFF00, not 0xFF<<8 = 0x7F80.
2026-04-16 11:07:56 +05:45
JunghwanNA a9ceb3c851 fix(cosim): align golden_reference ADC sign conversion with RTL
The golden reference used (adc_val - 128) << 9 which subtracts 65536,
but the Verilog RTL computes {1'b0,adc,9'b0} - {1'b0,8'hFF,9'b0}/2
which subtracts 0xFF00 = 65280. This creates a constant 256-LSB DC
offset between the golden reference and RTL for all 256 ADC values.

The bit-accurate model in fpga_model.py already uses the correct RTL
formula. This aligns golden_reference.py to match.

Verified: all 256 ADC input values now produce zero offset against
fpga_model.py.
2026-04-16 12:27:02 +09:00
Jason db4e73577e fix: use authoritative tx frame signal for frame sync, consistent ad9523 error path
FPGA-001: The previous fix derived frame boundaries from chirp_counter==0,
but that counter comes from plfm_chirp_controller_enhanced which overflows
to N (not wrapping at chirps_per_elev). This caused frame pulses only on
6-bit rollover (every 64 chirps) instead of every N chirps. Now wires the
CDC-synchronized tx_new_chirp_frame_sync signal from the transmitter into
radar_receiver_final, giving correct per-frame timing for any N.

STM32-004: Changed ad9523_init() failure path from Error_Handler() to
return -1, matching the pattern used by ad9523_setup() and ad9523_status()
in the same function. Both halt the system, but return -1 keeps IRQs
enabled for diagnostic output.
2026-04-16 00:33:27 +05:45
Jason 063fa081fe fix: FPGA timing margins (WNS +0.002→+0.080ns) + 11 bug fixes from code review
FPGA timing (400MHz domain WNS: +0.339ns, was +0.002ns):
- DONT_TOUCH on BUFG to prevent AggressiveExplore cascade replication
- NCO→mixer pipeline registers break critical 1.5ns route
- Clock uncertainty reduced 200ps→100ps (adequate guardband)
- Updated golden/cosim references for +1 cycle pipeline latency

STM32 bug fixes:
- Guard uint32_t underflow in processStartFlag (length<4)
- Replace unbounded strcat in getSystemStatusForGUI with snprintf
- Early-return error masking in checkSystemHealth
- Add HAL_Delay in emergency blink loop

GUI bug fixes:
- Remove 0x03 from _HARDWARE_ONLY_OPCODES (was in both sets)
- Wire real error count in V7 diagnostics panel
- Fix _stop_demo showing 'Live' label during replay mode

FPGA comment fixes + CI: add test_v7.py to pytest command

Vivado build 50t passed: 0 failing endpoints, WHS=+0.056ns
2026-04-14 00:08:26 +05:45
Jason b4d1869582 fix: 9 bugs from code review — RTL sign-ext & snapshot, thread safety, protocol fixes
- rx_gain_control.v: sign-extension fix ({agc_gain[3],agc_gain} not {1'b0,agc_gain})
  + inclusive frame_boundary snapshot via combinational helpers (Bug #7)
- v7/dashboard.py: Qt thread-safe logging via pyqtSignal bridge (Bug #1)
  + table headers corrected to 'Range (m)' / 'Velocity (m/s)' (Bug #2)
- main.cpp: guard outerAgc.applyGain() with if(outerAgc.enabled) (Bug #3)
- radar_protocol.py: replay L1 threshold detection when CFAR disabled (Bug #4)
  + IndexError guard in replay open (Bug #5) + AGC opcodes in _HARDWARE_ONLY_OPCODES
- radar_dashboard.py: AGC monitor attribute name fixes (3 labels)
- tb_rx_gain_control.v: Tests 17-19 (sign-ext, simultaneous valid+boundary, enable toggle)
- tb_cross_layer_ft2232h.v: AGC opcode vectors 0x28-0x2C in Exercise A (Bug #6)

Vivado 50T build verified: WNS=+0.002ns, WHS=+0.028ns — all timing constraints met.
All tests pass: MCU 21/21, GUI 120/120, cross-layer 29/29, FPGA 25/25 (68 checks).
2026-04-13 23:35:10 +05:45
Jason ffba27a10a feat: hybrid AGC (FPGA phases 1-3 + GUI phase 6) with timing fix
FPGA:
- rx_gain_control.v rewritten: per-frame peak/saturation tracking,
  auto-shift AGC with attack/decay/holdoff, signed gain -7 to +7
- New registers 0x28-0x2C (agc_enable/target/attack/decay/holdoff)
- status_words[4] carries AGC metrics (gain, peak, sat_count, enable)
- DIG_5 GPIO outputs saturation flag for STM32 outer loop
- Both USB interfaces (FT601 + FT2232H) updated with AGC status ports

Timing fix (WNS +0.001ns -> +0.045ns, 45x improvement):
- CIC max_fanout 4->16 on valid pipeline registers
- +200ps setup uncertainty on 400MHz domain
- ExtraNetDelay_high placement + AggressiveExplore routing

GUI:
- AGC opcodes + status parsing in radar_protocol.py
- AGC control groups in both tkinter and V7 PyQt dashboards
- 11 new AGC tests (103/103 GUI tests pass)

Cross-layer:
- AGC opcodes/defaults/status assertions added (29/29 pass)
- contract_parser.py: fixed comment stripping in concat parser

All tests green: 25 FPGA + 103 GUI + 29 cross-layer = 157 pass
2026-04-13 19:24:11 +05:45
Jason 2106e24952 fix: enforce strict ruff lint (17 rule sets) across entire repo
- Expand ruff config from E/F to 17 rule sets (B, RUF, SIM, PIE, T20,
  ARG, ERA, A, BLE, RET, ISC, TCH, UP, C4, PERF)
- Fix 907 lint errors across all Python files (GUI, FPGA cosim,
  schematics scripts, simulations, utilities, tools)
- Replace all blind except-Exception with specific exception types
- Remove commented-out dead code (ERA001) from cosim/simulation files
- Modernize typing: deprecated typing.List/Dict/Tuple to builtins
- Fix unused args/loop vars, ambiguous unicode, perf anti-patterns
- Delete legacy GUI files V1-V4
- Add V7 test suite, requirements files
- All CI jobs pass: ruff (0 errors), py_compile, pytest (92/92),
  MCU tests (20/20), FPGA regression (25/25)
2026-04-12 14:21:03 +05:45
Jason 519c95f452 fix: regenerate golden hex for dual-16pt Doppler and add real-data TBs to regression
Regenerate all real-data golden reference hex files against the current
dual 16-point FFT Doppler architecture (staggered-PRI sub-frames).
The old hex files were generated against the previous 32-point single-FFT
architecture and caused 2048/2048 mismatches in both strict real-data TBs.

Changes:
- Regenerate doppler_ref_i/q.hex, fullchain_doppler_ref_i/q.hex, and all
  downstream golden files (MTI, DC notch, CFAR) via golden_reference.py
- Add tb_doppler_realdata (exact-match, ADI CN0566 data) to regression
- Add tb_fullchain_realdata (exact-match, decim->Doppler chain) to regression
- Both TBs now pass: 2048/2048 bins exact match, MAX_ERROR=0
- Update CI comment: 23 -> 25 testbenches
- Fill in STALE_NOTICE.md with regeneration instructions

Regression: 25/25 pass, 0 fail, 0 skip. ruff check: 0 errors.
2026-04-09 02:36:14 +03:00
Jason 11aa590cf2 fix: full-repo ruff lint cleanup and CI migration to uv
Resolve all 374 ruff errors across 36 Python files (E501, E702, E722,
E741, F821, F841, invalid-syntax) bringing `ruff check .` to zero
errors repo-wide with line-length=100.

Rewrite CI workflow to use uv for dependency management, whole-repo
`ruff check .`, py_compile syntax gate, and merged python-tests job.
Add pyproject.toml with ruff config and uv dependency groups.

CI structure proposed by hcm444.
2026-04-09 02:05:34 +03:00