Two stale-baseline events were never captured in earlier commits:
1. The FFT-1024 -> FFT-2048 merge (c668652) updated the testbench and
gen_mf_cosim_golden.py but left radar_scene.py FFT_SIZE=1024. When
FFT_SIZE was later bumped to 2048, the input vectors written by
generate_baseband_samples (bb_mf_test_*.hex, ref_chirp_*.hex) grew
from 1024 to 2048 samples but were never re-exported.
2. The TX-I matched-filter realignment (5ff5671) changed the ADC chirp
phase from 2*pi*F_IF*t to 2*pi*(F_IF+F_BASEBAND_LOW)*t. ADC sample
values shifted from sample ~1336 onward but adc_*.hex was never
re-exported.
Result: every regression run produced a "dirty" working tree as the
regen reproduced post-merge values that disagreed with the committed
baselines. Two consecutive regen runs are bit-exact identical
(LCG seed=42 + deterministic chirp math) — verified via diff -q on
two output dirs. There is no actual non-determinism; only stale
artifacts.
This commit refreshes all 15 affected files in one shot:
- 6 input hex (adc_*_target.hex, bb_mf_test_*.hex, ref_chirp_*.hex)
- 5 RTL output csv (rtl_*.csv from current RTL)
- 4 compare csv (compare_mf_*.csv = py vs rtl side-by-side)
Verification: full regression 39/39 PASS on the refreshed inputs.
After this commit, regression runs should leave the working tree clean.
The DAC short/long chirp LUTs are 10..30 MHz upchirps (Hilbert-confirmed).
With TX_LO=10.500 GHz, RX_LO=10.380 GHz (adf4382a_manager.h) and the
120 MHz DDC NCO (ddc_400m.v), high-side mixing places the post-DDC echo
at 10..30 MHz baseband. The matched-filter reference (gen_chirp_mem.py)
was generating 0..20 MHz, implicitly assuming the chirp's low edge mixed
to DC. This caused a 10 MHz spectral offset and ~5 dB matched-filter loss.
Adds F_BASEBAND_LOW=10e6 in both gen_chirp_mem.py and radar_scene.py,
with phase formula 2*pi*F_BASEBAND_LOW*t + pi*rate*t^2 in all chirp
generators. Regenerates the 6 .mem files. Adds analyze_short_chirp_mismatch.py
for the Hilbert-based diagnosis. Fixes the misleading "30MHz to 10MHz"
comment in plfm_chirp_controller.v and adds an end-to-end frequency plan
in the LUT header.
Sideband orientation (high-side at both mixers) is the conventional choice
and consistent with antenna match (10.25..10.75 GHz, 8x16 patch designed
at 10.5 GHz). Loopback capture would settle definitively; if either mixer
is low-side the F_BASEBAND_LOW sign flips and/or chirp direction reverses.
latency_buffer.v has had zero non-tb instantiations since RX-B (2026-04-23)
replaced its hookup in radar_receiver_final with a 1-FF alignment register.
The module was being kept "for potential future use" — exactly the kind of
dead weight the codebase does not need. Deleted, along with all build /
test infrastructure that dragged it along:
- 9_Firmware/9_2_FPGA/latency_buffer.v
- 9_Firmware/9_2_FPGA/tb/tb_latency_buffer.v
- run_regression.sh: removed from RTL_FILES and RECEIVER_RTL
- scripts/200t/build_200t.tcl: removed from synthesis source list
- tb/tb_system_e2e.v: removed from header compile-string example
- tb/cosim/validate_mem_files.py: deleted test_latency_buffer() (~75 lines),
its call site, and the corresponding entry in the module docstring
Historical RX-B comments referencing latency_buffer in radar_receiver_final.v,
tb_rxb_fullchain_latency.v, and tb_rxb_latency_measure.v are kept — they
explain WHY the module was removed, which is still useful design archaeology.
Two doc-only housekeeping touches bundled in:
- plfm_chirp_controller.v: replaced two empty "CRITICAL FIX: Generate
valid signal" labels at LONG_CHIRP and SHORT_CHIRP with one shared
chirp_valid policy comment block above LONG_CHIRP that explains the
actual rationale (downstream FIFO underrun on trailing samples).
- v7/models.py: replaced the "range_resolution and velocity_resolution
should be calibrated" docstring (sounded like an open TODO but was a
documented placeholder) with a clear pointer to the GUI-C3 fix in
workers.py:RadarDataWorker so future readers know the live path
derives correct values from WaveformConfig.
FPGA quick regression unchanged: 28/29 (1 fail is the unrelated iverilog/
Xilinx-IP RX-NEW-3 gap). GUI suite 180/180. Ruff clean.
rx_final_doppler_out.csv is written by tb_radar_receiver_final.v on
every run via $fopen — it is a test-run artifact, not an oracle. It
was mistakenly tracked in an earlier commit, causing unnecessary
churn on every sim. Remove from the index and ignore going forward.
Also ignore stray a.out from iverilog one-shot compiles.
Golden references (.hex, .mem, doppler_golden_py_*.csv) remain
tracked — they are load-bearing oracles used by MF / Doppler /
receiver cosim testbenches.
RTL (P0 pre-bringup findings R-1/R-2/R-3/R-5/R-6):
- mti_canceller: add use_long_chirp input and waveform-boundary mute
so the long->short transition in mode 01 no longer subtracts across
heterogeneous waveforms (R-1). Prev buffer is overwritten in-flight
at the boundary so the next same-waveform chirp subtracts cleanly.
- ad9484_interface_400m: 2FF sync of mmcm_locked into the 400 MHz
domain before gating reset_n_gated (R-6).
- cic_decimator_4x_enhanced: correct max_fanout narrative (R-3).
- ad9484_interface_400m: strip stale pblock comment, note 3.0 ns
max_delay instead (R-2).
- mti_canceller / doppler_processor: 200T-20km WARNING banners
flagging the broken 4096-bin path (R-5). 9-bit BRAM address aliases
silently until rewritten.
- adc_clk_mmcm.xdc: relax set_max_delay from 2.700 -> 3.000 ns,
closes WNS with headroom on 50T build.
- radar_receiver_final: wire use_long_chirp into mti_inst.
Architecture-bump finalization (2048-pt range FFT, 512 range bins,
32 Doppler bins -> 16384 output cells per frame):
- tb/cosim/radar_scene.py: FFT_SIZE 1024 -> 2048, RANGE_BINS 64 -> 512.
- tb/gen_mf_golden_ref.py: N 1024 -> 2048.
- Regenerate all affected hex goldens (MF cases 1-4, Doppler inputs
+ py goldens, receiver integration golden_doppler.mem 2048 -> 16384).
- tb_radar_receiver_final: widen range_bin_out 6 -> 9 bits, bump
GOLDEN_ENTRIES 2048 -> 16384, expand bitmaps/arrays to 512 bins,
update all check messages and thresholds.
- tb_mti_canceller, tb_fullchain_mti_cfar_realdata: tie/pass
use_long_chirp so compile still works after RTL port add.
Test-suite hardening (coverage audit findings):
- tb_mti_canceller T12: 10 new assertions exercising R-1 waveform-
boundary mute across a long/long/short/short/long sequence. Catches
a regression that re-enables subtraction across the boundary.
- tb_fir_lowpass: replace tautological check(1'b1, ...) on coefficient
symmetry with a real hierarchical check coeff[k]===coeff[31-k];
replace always-pass overflow check with a well-driven (not X/Z)
assertion on filter_overflow.
- tb_matched_filter_processing_chain: replace three always-pass peak-
bin placeholders with peak-to-mean-|out| > 2x ratio checks (catches
flat/zero output that the old tautologies silently accepted).
- tb_cdc_modules M2: replace always-pass narrow-pulse check with a
well-defined-output assertion on the synchronizer.
- tb_nco_400m: replace always-pass freq-switch check with a swing +
no-X assertion across 200 post-switch samples.
- tb_system_e2e G12.1: replace check(1, ...) with test_num > 20 so
it catches a stalled TB that skipped prior groups.
- tb_multiseg_cosim TEST 4: replace always-pass placeholder with a
bitmap that asserts segment_request visited all 4 values.
- tb_mf_chain_synth and tb_fullchain_mti_cfar_realdata: add DEPRECATED
headers plus \$fatal guards (ifndef ALLOW_STALE_*) so they cannot
be silently re-enabled in CI with stale 1024-bin goldens against
current 2048-pt RTL.
Regression: 32 passed, 0 failed. MTI TB grew 30 -> 39 checks;
receiver integration grew 17 -> 18 checks with 16384/16384 golden
match at tolerance +/- 2 LSB.
Replace direct !reset_n async sense with a registered active-high reset_h
(max_fanout=50) in nco_400m_enhanced, cic_decimator_4x_enhanced, and
ddc_400m. The prior single-LUT1 / 700+ load net was the root cause of
WNS=-0.626 ns in the 400 MHz clock domain on the xc7a50t build. Vivado
replicates the constrained register into ≈14 regional copies, each driving
≤50 loads, closing timing at 2.5 ns.
Change radar_system_top default USB_MODE from 0 (FT601) to 1 (FT2232H).
FT601 remains available for the 200T premium board via explicit parameter
override; the 50T production wrapper already hard-codes USB_MODE=1.
Regression: add usb_data_interface_ft2232h.v to PROD_RTL lint list and
both system-top TB compile commands; fix legacy radar_system_tb hierarchical
probe from gen_ft601.usb_inst to gen_ft2232h.usb_inst.
Golden reference files (rtl_bb_dc.csv, rx_final_doppler_out.csv,
golden_doppler.mem) regenerated to reflect the +1-cycle registered-reset
boundary behaviour; Receiver golden-compare passes 18/18 checks.
All 25 regression tests pass (0 failures, 0 skipped).
Co-Authored-By: Claude Sonnet 4.6 <noreply@anthropic.com>
golden_reference.py: update comment from 'Simplified' to 'Exact' to
match shaun0927's corrected formula.
fpga_model.py: fix adc_to_signed docstring that incorrectly derived
0x7F80 instead of 0xFF00. Verilog '/' binds tighter than '-', so
{1'b0,8'hFF,9'b0}/2 = 0x1FE00/2 = 0xFF00, not 0xFF<<8 = 0x7F80.
The golden reference used (adc_val - 128) << 9 which subtracts 65536,
but the Verilog RTL computes {1'b0,adc,9'b0} - {1'b0,8'hFF,9'b0}/2
which subtracts 0xFF00 = 65280. This creates a constant 256-LSB DC
offset between the golden reference and RTL for all 256 ADC values.
The bit-accurate model in fpga_model.py already uses the correct RTL
formula. This aligns golden_reference.py to match.
Verified: all 256 ADC input values now produce zero offset against
fpga_model.py.
Regenerate all real-data golden reference hex files against the current
dual 16-point FFT Doppler architecture (staggered-PRI sub-frames).
The old hex files were generated against the previous 32-point single-FFT
architecture and caused 2048/2048 mismatches in both strict real-data TBs.
Changes:
- Regenerate doppler_ref_i/q.hex, fullchain_doppler_ref_i/q.hex, and all
downstream golden files (MTI, DC notch, CFAR) via golden_reference.py
- Add tb_doppler_realdata (exact-match, ADI CN0566 data) to regression
- Add tb_fullchain_realdata (exact-match, decim->Doppler chain) to regression
- Both TBs now pass: 2048/2048 bins exact match, MAX_ERROR=0
- Update CI comment: 23 -> 25 testbenches
- Fill in STALE_NOTICE.md with regeneration instructions
Regression: 25/25 pass, 0 fail, 0 skip. ruff check: 0 errors.
Resolve all 374 ruff errors across 36 Python files (E501, E702, E722,
E741, F821, F841, invalid-syntax) bringing `ruff check .` to zero
errors repo-wide with line-length=100.
Rewrite CI workflow to use uv for dependency management, whole-repo
`ruff check .`, py_compile syntax gate, and merged python-tests job.
Add pyproject.toml with ruff config and uv dependency groups.
CI structure proposed by hcm444.
- Remove xfft_32.v, tb_xfft_32.v, and fft_twiddle_32.mem (dead code
since PR #33 moved Doppler to dual 16-pt FFT architecture)
- Update run_regression.sh: xfft_16 in PROD_RTL, remove xfft_32 from
EXTRA_RTL and all compile commands
- Update tb_fft_engine.v to test with N=16 / fft_twiddle_16.mem
- Update validate_mem_files.py: validate fft_twiddle_16.mem instead of 32
- Update testbenches and golden data from main_cleanup branch to match
dual-16 architecture (tb_doppler_cosim, tb_doppler_realdata,
tb_fullchain_realdata, tb_fullchain_mti_cfar_realdata, tb_system_e2e,
radar_receiver_final, golden_doppler.mem)
- Update CONTRIBUTING.md with full regression test instructions covering
FPGA, MCU, GUI, co-simulation, and formal verification
Regression: 23/23 FPGA, 20/20 MCU, 57/58 GUI, 56/56 mem validation,
all co-sim scenarios PASS.
- radar_system_top.v: DC notch now masks to dop_bin[3:0] per sub-frame so both sub-frames get their DC zeroed correctly; rename DOPPLER_FFT_SIZE → DOPPLER_FRAME_CHIRPS to avoid confusion with the per-FFT size (now 16)
- radar_dashboard.py: remove fftshift (crosses sub-frame boundary), display raw Doppler bins, remove dead velocity constants
- golden_reference.py: model dual 16-pt FFT with per-sub-frame Hamming window, update DC notch and CFAR to match RTL
- fv_doppler_processor.sby: reference xfft_16.v / fft_twiddle_16.mem, raise BMC depth to 512 and cover to 1024
- fv_radar_mode_controller.sby: raise cover depth to 600
- fv_radar_mode_controller.v: pin cfg_* to reduced constants (documented as single-config proof), fix Property 5 mode guard, strengthen Cover 1
- STALE_NOTICE.md: document that real-data hex files are stale and need regeneration with external dataset
Closes#39
- usb_data_interface.v: Add 3 self-test status inputs, expand status packet
from 7 words (header + 5 data + footer) to 8 words (header + 6 data + footer).
New status_words[5] carries {busy, detail[7:0], flags[4:0]}.
- radar_system_top.v: Wire self_test_flags_latched, self_test_detail_latched,
self_test_busy to usb_data_interface ports. Add opcode 0x31 as status
readback alias so host can read self-test results.
- tb_usb_data_interface.v: Add self-test port connections, verify word 5 in
Group 16, add Group 18 (busy flag + partial failure variant). 81 checks pass.
- run_regression.sh: Add fpga_self_test.v to PROD_RTL lint list and system-
level compile lists. Add tb_fpga_self_test as Phase 1 unit test.
- 24/24 regression tests pass, lint clean (0 errors, 4 advisory warnings).
RTL fixes discovered via new end-to-end testbench:
- plfm_chirp_controller: TX/RX mixer enables now mutually exclusive
by FSM state (Fix#4), preventing simultaneous TX+RX activation
- usb_data_interface: stream control reset default 3'b001 (range-only),
added doppler/cfar data_pending sticky flags, write FSM triggers on
range_valid only — eliminates startup deadlock (Fix#5)
- radar_receiver_final: STM32 toggle signals wired through for mode-00
pass-through, dynamic frame detection via host_chirps_per_elev
- radar_system_top: STM32 toggle signal wiring to receiver instance
- chirp_memory_loader_param: explicit readmemh range for short chirp
Test infrastructure:
- New tb_system_e2e.v: 46 checks across 12 groups (reset, TX, safety,
RX, USB R/W, CDC, beam scanning, reset recovery, stream control,
latency budgets, watchdog)
- tb_usb_data_interface: Tests 21/22/56 updated for data_pending
architecture (preload flags, verify consumption instead of state)
- tb_chirp_controller: mixer tests T7.1/T7.2 updated for Fix#4
- run_regression.sh: PASS/FAIL regex fixed to match only [PASS]/[FAIL]
markers, added E2E test entry
- Updated rx_final_doppler_out.csv golden data
Adds two-layer lint pass (iverilog -Wall + custom static checks) that
catches part-select OOB errors and case-without-default warnings before
pushing to remote Vivado. Catches the exact Synth 8-524 class error that
broke Build 18 initial attempt. Lint errors abort regression; warnings
are advisory. Regenerated golden data for BRAM-migrated matched filter.
CDC fixes across 6 RTL files based on post-implementation report_cdc analysis:
- P0: sync stm32_mixers_enable and new_chirp_pulse to clk_120m via toggle CDC
in radar_transmitter, add ft601 reset synchronizer and USB holding
registers with proper edge detection in usb_data_interface
- P1: add ASYNC_REG to edge_detector, convert new_chirp_frame to toggle CDC,
fix USB valid edge detect to use fully-synced signal
- P2: register Gray encoding in cdc_adc_to_processing source domain, sync
ft601_txe and stm32_mixers_enable for status_reg in radar_system_top
- Safety: add in_bin_count overflow guard in range_bin_decimator to prevent
downstream BRAM corruption
All 13 regression test suites pass (159 individual tests).
New testbenches:
- tb_latency_buffer.v: 13/13 tests for BRAM delay line (P1-3)
- tb_cdc_modules.v: 27/27 tests for all 3 CDC primitives (P1-4)
- tb_ad9484_xsim.v: XSim testbench for AD9484 with Xilinx BUFIO/IDDR
- tb_nco_xsim.v: XSim testbench for NCO DSP48E1 path verification
Fixes:
- tb_usb_data_interface.v: updated test 33 from divide-by-2 check to
ODDR-style clock forwarding verification (39/39 pass)
- rx_final_doppler_out.csv: updated golden reference after bug fixes
RTL fix: matched_filter_multi_segment.v ST_WAIT_FFT now waits for
processing chain to complete ALL 1024 outputs and return to IDLE
before advancing to next segment. Previously, it transitioned on the
first fft_pc_valid edge, causing the chain to still be outputting
while multi-seg started collecting data for the next segment. This
broke the handshake and caused permanent deadlock after segment 0.
Also fixes forward reference of sample_addr_from_chain in
radar_receiver_final.v (declaration moved before first use).
New files:
- tb/tb_radar_receiver_final.v: P0 integration test for full RX
pipeline (ADC->DDC->MF->range_bin_decimator->doppler), 10 checks
- tb/ad9484_interface_400m_stub.v: behavioral ADC stub for iverilog
All existing tests still pass: multi-seg 32/32, MF co-sim 3/3,
Doppler co-sim 14/14.
Bit-accurate Python model (fpga_model.py) mirrors full DDC RTL chain:
NCO -> mixer -> CIC -> FIR with exact fixed-point arithmetic matching
RTL DSP48E1 pipeline behavior including CREG=1 delay on CIC int_0.
Synthetic radar scene generator (radar_scene.py) produces ADC test
vectors for 5 scenarios: DC, single target (500m), multi-target (5),
noise-only, and 1 MHz sine wave.
DDC co-sim testbench (tb_ddc_cosim.v) feeds hex vectors through RTL
DDC and exports baseband I/Q to CSV. All 5 scenarios compile and run
with Icarus Verilog (iverilog -g2001 -DSIMULATION).
Comparison framework (compare.py) validates Python vs RTL using
statistical metrics (RMS ratio, DC offset, peak ratio) rather than
exact sample match due to RTL LFSR phase dithering. Results: 5/5 PASS.